So, a couple weeks ago I made a few minor changes. Found out my intake pipe was too long & the coupler looking like it was jacked up was in fact jacked up. I didn't think it was jacked up but Moncef thought it was jacked up and yeah, I guess it was pretty jacked up. After dealing with this I thought, what other details did my dumbass fail to pay attention to? Looked over the exhaust and found a few. Several pipes were not lined up well along the flanges. Both cats were off quite a bit at the cat-to-invidia junction and several, really every damn pipe was off a little to a lot. A couple minor exhaust leaks as well. Couldn't hear them, but the carbon had visibly passed the gaskets.
After I made these corrections, I went out for a quick 0-60 and got a 5.6 @ 288'. Definite improvement from the last one.
After having done the intake mods above this week and driving the fx for a day, I went out for another 0-60 & got a 5.2 @ 278'. Same slightly inclined road every time. I figured it would perform better and it does. Three very noticeable things; 1. it gets off the line quicker, brake torque or not B. it wants more rpm 3. the exhaust note sounds smoother, little to no snap, crackle & pop.
I shifted later in this run than normal. The gauge is off 3-400 rpm and my redline's set at 6,900. I got lucky this run and must've just missed the rev limiter. It was about 32* during the run so I let the iat's get up a little to attempt to get the best comparison I could. I have a little more work to do with the throttle body and intake pipe this week. This weekend's supposed to be a little warmer, so I'll get another 0-60 but I also want a 60' time & hopefully another 1/4. Don't have any prior 60' times saved anywhere, so nothing to compare to except at the world's shittiest track last year where I got a 2.2, largely stock.
The 1st chart below is one that shows the supposed gains from the 75mm t.b. and the one below that is my last tune. I didn't know what to expect as I've seen a fair amount of negative results with the large t.b. but surmised that these guys fucked up somewhere along the line. Also, the NWP chart just doesn't scream vq35de to me and I still think there's something wrong with it but none of that matters now. I'm just glad I didn't waste my time and $ only to get little to no to negative results. No lean codes or vacuum leaks. No relearn procedures whatsoever with any of this shit I've done regarding the upper/lower collector or 75mm t.b..
Turns out my tuner is still in business which was great to hear. I'd like to get a dyno run in and maybe a little tuning on this setup before I install the headers but that's not practical. Improved times are what it's all about, damn the numbers, but I'm curious to see what the new chart's going to look like and if it'll benefit from adding fuel. The Tomei v2 headers are probably the only worth while shorty headers to install. Beyond these, the right long tubes but you'll get similar results with a good shorty & test pipe combo. I don't want my FX smelling like a lawn mower, nor do I want to draw attention from the po po, so I'm sticking with the high flows.
The Aramid iso-thermal spacer is like 5 or more stock gaskets stacked on top of each other. I don't know how minor a detail it takes to affect air flow good or bad, but this spacer adds a little length to the runners and actually helped the lower collector clear some of the b.s. I've got running underneath it from the wire tuck. As I mentioned above, it fits the intake manifold without overlapping runners unlike the stock gasket. I don't expect to see any difference in iat's due to the location of the maf. I bought the gasket on a whim, but I'm not convinced it will help because if the maf doesn't see the improvement, than neither does the ecu.
