Ed! Where have you been my brother? Yeah, 332 w/issues, not sure what that means with regards to final output but I am hopeful we can add on another 20-30 lbs when its running correctly. Maybe its close to finsl TQ #'s don't really know yet but the WHP #'s are lower than the before so the assumption is that everything will move up.
Was very pleaed to hear that the porting (intake/heads) is most likely not the culprit for the current issues. When it was done most of the work was removing ex casting/flashing and there was no deep dive material removal. I had thoughts of buying another intake to test etc. One lesson (and really I knew better) add on mods in sections or related groups, don't do it all at one rime as its much more difficult to track down problematic or underperforming parts. Replacing the bored TB was easy (not cheap) and cured a variety of issues, the moment we return to internal work the shit gets crazy again.
Car is being picked up Friday, techs will all study the dyno results and try to make a determination as to what wil be done. Best guess is removing, inspecting and re-instaling the cams.